This project was done over the summer just before leaving for my first year at Purdue in 2020. I decided to do this project mostly just for fun but also to get an introduction to some important skills like CAD and using electrical components such as switches, motors, etc. I was inspired by a YouTube channel that I had found recently at the time about making custom modifications to Nerf guns, so I thought I would take a crack at it myself.
Since the Nerf gun I chose to modify was an uncommon one, I didn't really have any reference to use on how to modify it. I started by opening it up to see how the mechanism works. As you can see from the
The plan was to design and print a custom shaft that would transmit the motor's drive through the gear train. A hole would be drilled through the shell so that the motor would have a direct line to the gear. The switch would be placed directly below the release trigger, so it would be easy to rev up and then shoot. A custom bracket piece was designed and printed to secure the motor in place while it was running.
During testing with the 3D printed shaft piece, all seemed to be working well initially, until the shaft started to melt. Fortunately, this was an easy fix. My good friend's dad has a drill press and a lathe in his garage, and so we were able to make a replacement out of aluminum.
After the electronic components had been put together, it was time to fire a few test shots. However, they weren't quite what I was looking for. The foam balls are so light, they lose speed quickly due to air resistance. I tried to improve on this feature by increasing the mass and by making them slightly more aerodynamic. I found a golf ball design on Thingiverse and 3D printed it in halves. The infill percentage was set higher than normal to give it more mass and make it more resistant to impacts. To my surprise, the plastic ball didn't even fire from the Nerf gun. Upon further inspection, it turns out that the foam balls are compressed slightly when they pass through the flywheel, and the soft material allowed them to fit through. The plastic ball was much more rigid, so it would get stuck and scraped up by the flywheel.
The results for this project weren't exactly what I was hoping for. It sounds quite powerful, but the foam balls don't get shot that far. While I think a more powerful motor would make a difference, it still