I completed this project in the summer of 2021 while assisting a graduate student in the Bioadaptive Morphology Laboratory (BAM Lab) at the University of Illinois Urbana-Champaign. His research revolved around making small, light gliders inspired by the geometry of grasshopper wings. A repeatable, consistent launcher was necessary in order to test the accuracy and flight distance of the various glider geometries.
The first step was to choose a method of launching the gliders. Their previous method used a rubber band that was pulled by a human and then released to propel the glider. That method had two main issues. The first is with the rubber band itself. The rubber band was not strong enough to give them the desired distances they wanted to test at, and it was not durable enough to launch enough times to get a sufficient amount of data. The second major issue was that the human component of the launch could give a lot of inconsistencies between launches. The person launching the gliders would have to make their best guess at where to pull the rubber band to, and the exact way they release their fingers may be different from launch to launch.
After doing some research, I was able to come up with solutions to these issues. The first would be to replace the rubber band with an elastic that is used in sewing applications. This elastic was much stronger
I used SolidWorks and the lab's 3D printers to rapidly prototype the two different designs until they were satisfactory. Then I gathered some data using glider dummies that didn't have wings to test the consistency of the launchers.
The electromagnet design was somewhat tricky to get working. Figuring out a way to attach a magnetic piece of material onto the elastic without having that piece interfere with or impact the glider during the launch was challenging. Because of this, I decided to launch the glider with the elastic oriented vertically, similar to a bow, so that the magnetic attachment could be placed above the glider. However, that presented other issues now that we had to thread the elastic through the guide rails. Eventually, the tolerances were figured out after multiple iterations of prototypes. Even after the elastic was able to slide between the guard rails without interference, the electromagnet appeared to not be strong enough to hold the elastic when it was pulled all the way back. The specifications on the website where the electromagnet was purchased from stated that it was more than capable of producing enough force. After some consideration, we found that the electromagnet was a lot weaker than its rating because of the poor contact with the magnetic attachment that was epoxied onto the elastic. This issue was resolved by adding a metal disc to the attachment to increase the surface area that was in contact with the electromagnet. Changing to the metal disc wasn't perfect, as the increase in volume and asymmetric nature led the elastic to spin and move more during the launch.
After doing the tests with the dummy gliders, the rod-based release system was found to be more
This project was my first time designing something with multiple parts that had to work together, so some of my initial designs had parts that didn't fit together properly or strongly enough. By the end, I had learned about some common ways to join parts together, and now take that into consideration heavily when designing parts. Another big issue I ran into on this project was the amount of time it took to order certain parts that I needed for the project. There were some parts that I was hesitant to order because I wasn't quite sure I would need them, but when I figured out exactly what I needed, I had to wait a few extra weeks. Now I know to order parts ahead of time, so that I'm not stuck waiting for them to progress the project.